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Then the motor itself had to come out because it causes self-induction when spun by my stepper motor, and this makes the rotation less smooth.
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And finally the bearing had to go. This involved an arbor press and a ball bearing to focus the force (and a hemostat to hold the ball bearing, which didn't actually work the first time — it's out there somewhere).
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Now it was time to make mount pads for the stepper motor and servo assembly. I felt like a tornado cutting through a trailer park as these little chips and things got in the path of this huge end mill.
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The original hole needed to match the mount ring on the stepper motor.
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And the original screw holes didn't align, of course.
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At this point, it looks like this, with the stepper motor firmly attached.
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The arm of the read/write head needed some rocket surgery. Only the top head is being used because it's the only one visible, so the others were eliminated.
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Now it's time to make standoff posts for the little servo that drives the arm. It's not designed to be mounted upside down, so I had to get creative. Here's trimming down 1/4" fiberglass rod to about 3/8" long. It's a carbide bit because fiberglass is rough on high-speed steel. This is the "vise in a vise" trick, where the little guy is sideways so the process is repeatable across all four standoffs.
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And there needs to be a hole for the mounting screw.
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All four ended up like this.
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And they attach this way.
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The servo can now be mounted quite nicely.
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The head assembly needed a small hole for the drive shaft. I broke three bits doing this. Not only is that a waste, but they each got stuck in the assembly, which meant I had to drill the next one slightly off target.
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